Building Description
L4500 is a critical 24/7 Flight Simulator
Training Facility with one supporting Data Room, Administrative
Offices, Training and Conference areas and Dorm Rooms to house
the troops being flight trained. As would be expected of such
a facility, the HVAC requirements of the various areas differ
significantly.
The HVAC system consists of:
- The central plant included two water chillers with associated
pumps and cooling towers, and is primary-secondary pumped
and piped. All pumps were constant volume, and the cooling
tower fans were equipped with variable frequency drives.
- The hot water system is comprised of one boiler and associated
pumps and provides space heating used for Data Rooms’ humidity
control (reheat) and zone heating.
- 8 central station air handling units, one of which is constant
volume, the VAV air handling units serves the VAV boxes in
the office/training areas. All air handling units used inlet
guide vanes for capacity control, and all were equipped with
100% outside air economizers.
- 75 room fan coil units located in each Dorm room.
- 4 chilled water/hot water computer room a/c (CRAC) units
serving the Data Rooms
- Incomplete direct digitally controlled EMS.
Project Problems/Issues
- 30 year old central plant, no automation or energy conservation
capabilities, lack of redundancy and excessive maintenance
costs
- Dilapidated air handling units, most equipped with inlet
guide vanes. Most control valve, damper and inlet guide vane
actuators were inoperable
- 2-pipe system serving the Dorm Rooms resulted in constant
comfort complaints
- General lack of energy management capabilities
- Inability to provide accurate and repeatable temperature
and humidity control to the newly installed Data Room serving
the newly installed Simulator
Project Overview
Energy-Environment-Economics
provided a detailed engineering study and report of the HVAC
System’s current (existing) condition and operation including:
HVAC system design and DDC system deficiencies, potential energy
conservation opportunities with budgeted project costs and economic
analysis, and maintenance related operational and efficiency
analysis. The result of this study became an approximately $1,000,000
Energy Conservation Project including Retro-Commissioning and
OptimissioningSM - a combination of HVAC system commissioning
and optimization - of the facility. The project included the
engineering required for the modernization and automation of
the chilled water central plant and the air distribution system.
Also, project coordination and test & balance services were
provided in addition to the commissioning and optimization services
provided.
Solutions Provided
The study quantified in great detail the extent
of deterioration of the HVAC system, identified existing maintenance
deficiencies and generated schematic designs with cost estimates
to repair and modernize the system. These estimates were used
to provide the economic justification to move the project forward,
as energy conservation potential, reliability concerns, and
avoided maintenance costs made modernizing the HVAC system fiscally
responsible. However, the critical nature of the facility and
the required scope of work to implement the recommendations
mandated precise scheduling and provision of temporary utilities.
So in addition to providing the final construction documents,
Energy-Environment-Economics also provided project coordination
services, eliminating the need and additional cost for a general
contractor. Preparation of the construction documents was critical
to meeting the project’s energy conservation goals, maintaining
the schedule and meeting budget requirements, so Energy-Environment-Economics
worked closely with equipment suppliers to generate precise
pre-purchase specifications for the new central plant equipment
and air handling units. To reduce construction costs, the new
air handling units were designed to utilize the existing roof
curbs, eliminating any roofing costs or potential risks.
Because the facility’s loads had increased significantly over
30 years, and the central plant was going to incorporate a hydronic
economizer capability, the air handling units were increased
in airflow and coil size and capacity. Larger coils result in
lower pressure drops and required fan HP, but also result in
lower velocities and closer approach temperatures that extend
the potential for operating in hydronic economizer mode. The
air handling units were equipped with factory installed variable
frequency drives, and new pressure independent control valves
were installed inside the air handling units’ pipe vestibules
to protect them from the weather.
These specific control valves were part of the overall central
plant modernization plan, and were important to final chilled
water coil selection criteria. Because low chilled water system
temperature differentials (DT) result in capacity loss and increased
energy costs, and because redundancy was critical to the uninterrupted
operations of the facility, the valves and chilled water coils
were carefully selected to compliment the new central plant
design. The design intent was to provide 100% redundant capacity
in the chillers, pumps and cooling towers, and the design day
load was calculated exactly and did not contain any typical
safety factors, so the chilled water system’s correct operation
– at a minimum maintaining the design (12degrees) DT - was of
the utmost importance.
Demolition of the central plant began after a temporary air-cooled
chiller, with power provided from abandoned circuits, was installed
to provide temporary cooling to critical areas. Once demolished,
construction of the new state of the art variable flow primary
only chilled water central plant began. Three new chiller modules
were provided, and a dual circuited fluid cooler was installed
to serve the dual purpose of heat rejection during chiller mode
as well as act as the hydronic economizer. Eight new automated
control valves were added, as was a flow measuring station and
bypass valve intended to ensure a minimum flow rate to the chiller
during low load periods if needed.
Because each of the fluid cooler’s circuits were sized for
a design day, and that the entire tube bundle was to be used
during hydronic economizer( heat exchanger) mode, a chiller
low flow condition was unlikely. In addition to the large surface
area of the fluid cooler’s tube bundle, the condenser water
pumps were equipped with variable frequency drives that would
modulate to provide and maintain the chilled water system’s
differential pressure setpoint during heat exchanger mode, as
the chilled water/condenser water system is now one closed loop.
During heat exchanger mode only the condenser water pump operates,
variably, reducing flow rates and velocities thru the tube bundle.
The extended surface and reduced velocities create conditions
where we have achieved 2-degree approaches between ambient wet-bulb
(WB) temperatures and leaving “chilled” (in heat exchanger mode)
water temperatures. In a typical open cooling tower/plate/frame
heat exchanger/constant volume condenser water pumping system
a 10-degree approach would be more common.
Obviously this capability greatly extends the hours when economizer
mode is available to be used, even considering the sensitive
nature of the Data Room’s temperature and humidity requirements.
It also allowed us to stage – if needed – one of the two air
handling units dedicated to the Simulator Bay on or off according
to need. Prior to OptimissioningSM both existing air handling
units operated 24/7 in a constant volume mode. Our analysis
and carefully selected air handling units now cycle as needed,
and were converted into a single zone VAV configuration to save
even more energy.
To complement the new HVAC system’s capabilities, new EMS
algorithms were written and all vital system setpoints were
optimized for maximum energy efficiency. Innovative reset schedules
for chiller and heat exchanger modes of operations were devised
and implemented, and Energy-Environment-Economics Test &
Balance services were used to optimize the control setpoints
and reset schedules of the air handling units. While not the
prime focus of the project, the hot water system was outfitted
with reset schedules to save energy but also to reduce the constant
complaints of the Dorm occupants due to the either cooling or
heating capability of the 2-pipe system serving that area of
the facility.